After my morning coffee break I stopped by the old school to check on the flying field that has been locked since construction went sour. The prime contractor didn't bother paying the subs so they left and nobody worked on the school for some time. Work is going again and I have access to the field again. I returned with a push mower and carved out a circle and got in some flights with the .25 powered Ringmaster. Strange engine runs. I set it on the ground at a fast 4 cycle and as it started to move the engine would go wide open and stay there for the flight. I richened it more and more each flight but nothing changed. I went to the dog track today with it and the same thing happened. I richened it a turn and for 2 minutes it ran rich. Too rich to do anything but then it went lean again. I removed the tank and installed a plastic clunker. There isn't any way to to add a uniflow tube but then I figured it out. I poked a hole in the end with an awl and jammed a pipe in. I set it above the engine c/l and will test it next time out. The winds today are light and variable. Not at all good for control line flying. Any way the Fox .25, that I got off ebay, seems to be more than enough for the Ringmaster. I want to try it on a Primary Force when I get it running right.
I sold 9 items on ebay yesterday. 2 left to ship.
Wednesday, November 12, 2008
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